8/24/2012 Sunrise Aviation Flight School Airplane Crashes at Ormond Beach Airport.

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Additional information:

 

NTSB Identification: ERA12LA525
14 CFR Part 91: General Aviation
Accident occurred Friday, August 24, 2012 in Ormond Beach, FL
Aircraft: CESSNA 152, registration: N24264
Injuries: 1 Uninjured.

 

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On August 24, 2012, at 0926 eastern daylight time, a Cessna 152, N24264, was substantially damaged when it overran the runway during an aborted takeoff at Ormond Beach Municipal Airport (OMN), Ormond Beach, Florida. The private pilot was not injured. Visual meteorological conditions prevailed, and a visual flight rules flight plan was filed from OMN to Gainesville Regional Airport (GNV), Gainesville, Florida. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.

According to the pilot, the engine performed "normally" during taxi and the before takeoff checks. After the airplane rotated during the takeoff, he felt that it was not climbing, so he decided to make an emergency landing.

According to a Federal Aviation Administration (FAA) inspector, the airplane came to rest about 625 feet beyond the departure end of runway 8. The throttle was found in the maximum power position, the mixture was full rich, and carburetor heat was off. There was some stiffness noted when moving the throttle control; however, the carburetor was broken off the engine at the mounting flange. Both propeller blades were bent.

Engine rotation produced spark on all spark plug leads and compression on all cylinders. Engine cold cylinder compressions were between 70 and 77 psi. The top spark plugs were removed from all cylinders, and upon visual inspection, indicated "normal" burn.

Fuel samples were absent of debris, and no water was found in the fuel tank sumps, gascolater or carburetor float bowl.

The inspector spoke to flight instructors who flew the airplane on the two previous flights, who stated that its performance was "normal" during those flights. The inspector also spoke to the to the tower controller, who related that the airplane lifted off and settled back down on the 4,005-foot runway twice before overrunning the departure end.

Winds, recorded at the airport about the time of the accident, were calm.